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高压加热器解列及投运分析
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(1.中国核工业集团有限公司集团办公室,北京 100045;2.江苏核电有限公司运行三处,江苏连云港 222000)

作者简介:

彭福祥,男,1994年生,工程师,从事核电机组日常运行 监测、参数调整、系统操作以及工况风险研判工作,E-mail: pengfuxiang@cnnc.com.cn。

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Analysis of Isolation and Putting into Operation of High-Pressure Heater
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(1. Secretariat,China National Nuclear Corporation,Beijing 100045,China;2. Third Operations Branch,Jiangsu Nuclear Power Corporation,Lianyungang,Jiangsu 222000,China)

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    摘要:

    田湾核电站 5号机组在调试期间,高压加热器解列后重新投运时频繁出现水位异常升高并触发保护解列。为解决该问题,分析系统结构与疏水控制逻辑,采用列举排除法排查故障原因,确认疏水闪蒸是导致虚假高水位的根本诱因。基于此,提出优化投运操作、调整疏水定值、完善监测与控制逻辑等措施。经现场验证,该措施可有效避免水位异常波动,保障加热器平稳投运,可为同类机组高压加热器运行优化提供一定参考。

    Abstract:

    During the commissioning period of Unit 5 of Tianwan Nuclear Power Plant,the high-pressure heater frequentlyexperienced abnormal water level rise and triggered protection disconnection when it is put back into operation after beingdisconnected. To solve this problem,this paper analyzes the system structure and hydrophobic control logic,uses the enumeration elimination method to investigate the cause of the fault,and confirms that hydrophobic flash evaporation is the fundamental cause of the false high water level. Based on this,measures such as optimizing operation,adjusting drainage settings,and improving monitoring and control logic are proposed. Through on-site verification,this measure can effectively avoid abnormal fluctuations in water level,ensure smooth operation of the heater,and provide certain reference for optimizing the operation of high-pressure heaters in similar units.

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  • 在线发布日期: 2026-06-03
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